So anyway, two caps come in and I install them. Computer stops working.
I removed them, works again. Installed one of the two, works still. Installed the last, works still.
Never figured out why it did that, but it shows that weird voodoo like this can happen.
LOL... of course. I put one tantalum cap back on at a time and then plug everything back in to test the display. And test the continuity on each end of the cap with where it should be connected to. One by one. And of course, the display works after each cap is replaced and continues working even after the last one...
So they all work and it's all good now.
During the first attempt, I checked continuity from the tab on each end of each tantalum cap to the other component on the board it's connected to. And got good tone. That should have meant each cap was solidly connected to the board. I even used tweezers to nudge each cap to ensure it would not budge.
My hypothesis: I nudged each cap side to side... but that wasn't good enough as the other joint could have prevented it from moving side to side. I needed to also gently push down to see if there was any movement. I did not do that. And when I placed the probe on the tab to test, I must have pushed it enough to gain continuity for the test. Lesson learned.
Although I wasted many hours on debugging this, I'm glad it's working now. Will post some more pictures this weekend.
Final set of changes for this unit:
- Recapped the motherboard (single capacitor).
- Recapped the modem board.
- Recapped the inverter board.
- Recapped the display.
- Display now looks good, no more bleeding.
- Cleaned off corrosion on the magnesium frame and repainted it matte black with rustoleum paint (and ensured each ground contact point was sanded back to raw magnesium -- probably should have just masked it in hindsight).
- Replaced rusted screws all over the board (M2 and M2.5 button head screws).
- Repaired two standoffs that had broken tops -- 3d printed new washer like tops and epoxied them to the remaining part of the standoff (will share pictures later).
- 3D printed new two piece hinge standoffs and used M2.5 brass inserts instead of screwing into the plastic, and epoxied them into place.
- Added epoxy around remaining ok standoffs for added strength.
- Swapped out laptop SCSI drive with a ZuluSCSI laptop version.
Next step on this laptop will be to attempt a battery rebuild.
Back in my days racing RC cars, I built NIMH battery packs (AAA, AA, and sub-C) and soldered the tabs myself. I know most people go for spot welding these to prevent heat damage, but I never had an issue back in the day as long as you increase the temp on the soldering iron and only applied heat for a split second. I'm going to try and see what happens. If I fail, will figure out how to spot weld them.